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我厂总装车间发动机生产作业线具有生产批量大、劳动效率高、强制性强等特点。过去钻削飞轮定位销孔的排屑全靠人力翻转机体完成。由于发动机体积大而重,翻转排屑很困难,不仅费工费时,劳动强度大、效率低、而且很不安全,不能适应生产的需要,一度成为影响生产的突出问题。针对此种情况,该车间工人师傅自己动手,利用废旧料革新制作成一种利用压缩空
Our factory assembly shop engine production line with production volume, high labor efficiency, mandatory and so on. In the past drilling flywheel positioning pin hole chip completely rely on human body to complete. As the engine is bulky and heavy, reversing the chip removal is very difficult. It not only takes time and labor, but also is labor-intensive, inefficient, and unsafe. It can not meet the needs of production and has become an outstanding problem affecting production. In view of this situation, the workshop workers master yourself, the use of scrap materials made of a new use of compressed air