某水库副坝坝基渗漏成因分析及渗透稳定性计算

来源 :水电能源科学 | 被引量 : 0次 | 上传用户:LoveYouNeverChange
下载到本地 , 更方便阅读
声明 : 本文档内容版权归属内容提供方 , 如果您对本文有版权争议 , 可与客服联系进行内容授权或下架
论文部分内容阅读
针对某水库副坝坝基长期存在的渗漏问题,在综合分析历次地质勘察结果的基础上,采用高密度电法对副坝进行无损探测,同时,采用有限元法对副坝渗流性态进行二维数值模拟,分析坝基渗漏对副坝渗透稳定性的影响。结果表明,副坝坝基渗漏主要是由于坝基存在强透水的砂砾石层;副坝坝基渗漏未彻底解决的主要原因是已采取的防渗措施不当或存在质量缺陷,1978~1979年实施的桩号0+678~0+700段沟槽防渗墙存在缺陷,2000年实施的灌浆效果不佳;防渗墙失效后,副坝坝基砂砾石层在校核洪水位工况下可能发生渗透破坏,建议进一步采用混凝土防渗墙对副坝坝基进行防渗加固处理。 Aiming at the long-term seepage problem of the dam foundation of a reservoir, based on the comprehensive analysis of previous geological survey results, the non-destructive detection of the auxiliary dam is carried out by using the high-density electrical method. Meanwhile, the seepage behavior of the auxiliary dam Dimension Numerical Simulation to Analyze the Influence of Dam Foundation Leakage on the Seepage Stability of the Auxiliary Dam. The results show that the seepage of the auxiliary dam foundation is mainly due to the strong water-permeable gravel layer in the dam foundation. The main reason for the incomplete settlement of the auxiliary dam foundation is the improper anti-seepage measures or quality defects, There is a defect in the seepage cutoff wall of station 0 + 678 ~ 0 + 700 and the poor grouting effect was implemented in 2000. After the seepage cutoff wall fails, infiltration of the subgrain dam foundation gravel layer may occur under the condition of checking flood level Destruction, it is recommended to further use of concrete cutoff wall of the secondary dam foundation seepage reinforcement.
其他文献
基于某矿一采区工作面巷道应力集中程度较高、具有煤岩突出危险征兆等问题,以该矿1303工作面运输平巷应力集中区为研究对象。通过数值模拟分析钻孔直径依次为50、75、108、12
一、现状 1、建国50年来我国污水处理行业的成长历程 (1)50—60年代的状况。解放初期由于工农业生产刚刚起步,当时的污水污染程度很低,且提倡利用污水进行农业灌溉,特别是北